Thursday, December 28, 2023

Tosten PTT switch replaced

The push to talk switch still worked but was requiring a bit more deliberate squeeze to transmit.  Probably the victim of abuse from of an occasionally white knuckled test pilot.  

The pilot's control stick was pulled apart to access the push to talk switch.   Tosten had mailed me instructions and a replacement circuit board with two switches on it.   Unfortunately, after popping the stick apart it was found that the circuit board didn't match my model, but the switches on the circuit boards were very similar.

The old button was unsoldered.   One of the good switches was unsoldered from the new board and replaced the old switch, then contacts were checked to ensure operation wasn't affected after being soldered back.

Reassembly is a bit of a challenge because the PTT trigger spring easily comes loose if the trigger moves when the switch halves are mated back together.  There were multiple lengths of screws holding the stick halves together so I made a mental note which ones went where and managed to get them back where they belonged.

The stick was reinstalled then tested.  

New charts were out so the memory cards were updated.







Monday, December 18, 2023

Buzzing around PK Lake

 

A filter capacitor helped reduce but not completely eliminate alternator whine audible on the GoPro videos.  CHT's are very close between pairs of cylinders but still vary quite a bit between the front and back cylinders depending on airspeed.  The old GoPro battery doesn't last very long so needs retired.



Take off from T67





PK Lake


Wednesday, December 13, 2023

Alternator whine

 My ARINC 429 module went off line again recently.   I'd made a few changes but became suspicious that dirty power is the culprit.   For some reason, I'd never put a filter cap on the alternator.  Last night I pulled up one of my videos on my iPad and the alternator whine was very audible.  On a few others, noise from the trim motors can be heard.  It didn't seem to be very noticeable when I watch it on a desktop and think it's because I don't turn the volume up very much on my PC.  Some of the videos are recorded with an audio cable connected to the copilot's receive audio and others are recorded using the GoPro's mic.   Also, I'm not hearing alternator whine in my headsets.  

The commercially available filter cap is 15 microfarads and connects directly to the B lead on the alternator.   I pulled some caps out of a PC power supply that were 470 uF and will try one of those connected at the engine buss fuse panel (which is much closer to the avionics).  


Update-flight and video seem to indicate the whine is reduced but pitch trim motor noise is still audible.  The ARINC module stayed on line.  CHT temps are

Dynon Electric Landing Gear configuration

My gear and canopy warning indications are through Dynon's EMS220 which give indications on the panel and audible warnings through the audio panel.  For the landing gear, I made a voltage divider circuit out of resistors and connected it to the yellow wire going to the landing gear switch, the other side of the voltage divider connects to ground and the middle wire goes to the EMS220 contact.  The voltage divider reduces 12 volts to less than 5 which is what the EMS220 contact I used is rated for. 

Functionally, the "Check Gear" and "Gear Overspeed" audible warnings work well with the caveat that it takes about 20 seconds for the gear to fully extend, so getting the "Check Gear" on final may require a go around if there's inadequate time to extend the gear.

The canopy warning uses a magnetic door reed switch and the latch lever as contacts to complete the circuit.  A file was created and loaded into the Dynon HDX that only warns audibly about the canopy if the RPM goes over 1900 RPM while the canopy not latched.

A quick video of the HDX setup for several widgets:

https://youtu.be/PRun_iBb4Hc

Here's an excerpt regarding the landing gear configuration from the Dynon Forum:

https://forum.flydynon.com/threads/landing-gear-up-warning.5098/

Make sure you're looking at the latest version of the manual. Here's the relevant excerpt from those pages:

Contacts Used for Retractable / Amphibious Landing Gear and Related Alerts
The simplest method to monitor landing gear state is to use a contact as there are only two states to monitor and it is mechanically and electrically easiest to install. To enable audio alerts related to landing gear status, the contact used for monitoring the status of landing gear must be named GEAR:
SETUP MENU > EMS SETUP > SENSOR INPUT MAPPING > C37 Pxx >
> FUNCTION: CONTACT
> SENSOR: CONTACT
> NAME: GEAR
To configure the GEAR contact alert for retractable landing gear:
Install the GEAR contact that when the landing gear is up, the state of the contact is UP and when the landing gear is down, the state of the contact is DOWN.
• SETUP MENU > AIRCRAFT INFORMATION:
> LANDING GEAR TYPE: RETRACT
> LANDING GEAR CHECK SPEED: (set as appropriate for your plane)
> LANDING GEAR OVERSPEED: (set as appropriate for your plane)
To configure the GEAR contact alert for amphibious landing gear:
• Install the GEAR contact that when the amphibious landing gear is configured for landing on water, the state of the contact is WATR and when the amphibious landing gear is configured for landing on land, the state of the contact is LAND.
• SETUP MENU > AIRCRAFT INFORMATION:
> LANDING GEAR TYPE: AMPHIB
> LANDING GEAR CHECK SPEED: (set as appropriate for your plane)
> LANDING GEAR OVERSPEED: (set as appropriate for your plane)
• SETUP MENU > SYSTEM SETUP > AUDIO SETUP > LANDING GEAR > VOICE


As for the actual annunciations, those are in the pilot's guide. Here's what you'll hear for each:

“Check Gear” : The aircraft is configured as a
Retractable gear, and the Landing
Gear is UP, and the aircraft is
descending through the configured
minimum warning speed.

“Gear Overspeed” :
The aircraft is configured as either a
retractable or amphibious gear, the
landing gear is not UP, and the
airspeed is exceeding the configured
maximum gear down speed.

Thursday, December 7, 2023

Vance Visits-Ardmore trip-squawks

 


Vance Atkinson came out to get a stack of aviation magazines I had saved for him and to get a long overdue flight in the Cozy.  

I pulled the 50 lbs. of  ballast out of the nose and dug out an old ANR headset, and adjusted seat foam.

We loaded up and headed North.  Vance took the controls and checked the stall speed, stick/pitch force etc.  He admired the panel and avionics capability.  He gave the controls back.  I zig zagged around Class B space, climbed to 5500 and headed direct to KADM Ardmore OK.   Unfortunately, my ARINC module had gone off line and I was seeing some other Dynon messages.   It's seeming to me like the transponder's RF is causing problems since one of the recent changes I made was to pull some shielding foil off the annular slot antenna.  I'll check electrical connections again to be sure nothing has loosened up again.   The tower cleared us to land on 17 but I had a brain fart when I saw a Cherokee doing a low approach on 13 and followed it.  Oops.   Tower called me and asked if I was on 13 and then gave taxi directions to the ramp.  5 of my neighbors had also flown up to Ardmore for lunch.  







Went WOT/Rich for a bit.  More work to do tweaking CHT's.  Probably need something that is adjustable in flight.

Vance noted that he couldn't hear my transmit audio when I talked on the radio.  I think the headset was set for mono and not stereo so will check that.  He could hear fine when we were talking on the intercom.  

I noticed that the belly brake switch had been flipped accidentally in flight, but fortunately the WOT switch on the throttle had latched the relay to keep the brake up.   I've had two pilots ride with me that bumped switches on the console so need to finish the switch protector before someone breaks a switch inadvertently.  I hadn't put the "protector" on because it isn't pretty, but for now it will be more prudent to install it.

The engine did start nicely although it had to crank a bit longer after the last SDS map tweak so maybe needs a touch more fuel on the start cycle table.


Vance approves!


Monday, December 4, 2023

Test flight - CHT balancing - VOR approach - Oscar Pattern

The SDS Fuel values were tweaked to remedy a rough idling after start issue and seemed to help.  Apparently my version 3 values were to rich for the cooler engine temps below 90F. 

Despite adding some deflectors to the lower cowl ramps, #1 is still the coolest.  I think I'm going to make something more adjustable and remove the deflectors.  I might try to see if there's a way to use a servo to adjust the ramp lips in flight.  Then find an optimal position and semi-permanently fix them there.  

I did a test flight from T67 to MWL via MQP (VOR to 31).   Everything seemed to work except for the VNAV/ILS.  As far as I can tell, the Dynon settings appear to be correct but I'll consult with a friend and adjust if necessary, then test again.  The nice thing is it did follow the approach.   Unfortunately, the pattern and RNAV approach was busy so left the area to the North.

I did about 75% of an Oscar pattern, and got disoriented but did a total of 3 360 turns/climbs and descents.  I spotted a tower nearby as I was descending so terminated the practice.  The radio traffic at Mineral Wells was still busy, so headed back to T67 rather than try another approach.





Sunday, December 3, 2023

Oil Analysis Lab tests ordered/Google cloud loses user data

 I've saved samples from oil changes but hadn't had them tested yet.   Another Cozy flier had chatted with me said that he's seeing ferrous metal in his last sample.  He prepaid for 6 tests and gave me a copy of his reports.  His recent oil change included his trip to Oshkosh/wet weather, so maybe the next sample will be clear.

When I change oil, I cut the filter open and look at it in the sunlight.  Recently I'd read where another way to check for ferrous metal was to rinse the pleats out with solvent, then use a magnet to pick up metal out of the solvent so I tried that this time.  There was just a tiny amount on the magnet.   I'd been helping a friend inspect his filters on a zero time 540 and had seen the first three or so filters have glitter sized specs of metal in them and after that just pieces of carbon and once it looked like a shaving of plastic from an oil bottle.

This morning I ordered the six pack lab test package from Blackstone-labs.  I've got samples from the last four oil changes to send in.

I'd been making log entries on Google Docs with separate documents for the airframe, engine and prop but not been keeping up as well with the physical hard copy logs.  I was wondering if it was worth the time to keep hard copies up to date anymore but this week, there was a tech article disclosing that Google had "lost" users data and had to do a restore dating back to earlier 2023.  I like having access on line.   I was in Houston when Dynon announced a safety of flight issue for the Autopilot Button module with specific serial numbers.  Having that info recorded in a log book in my shop wasn't as helpful as having access to it via the Internet.  It wasn't hard to boot the system up and read the serial number from the screen either. 


Weird....I found this entry and it says, "Published 12/3/23 9:31 AM" but it doesn't seem to be.....I'll hit the publish button again....





Friday, December 1, 2023

Balancemasters and other tweaks test flight

 Audibly, I couldn't tell much difference after putting on the balancer.  However, feeling the instrument panel definitely felt like the vibration was reduced.   Any rattling sound I'm hearing is resulting from the prop, cowl & turbulence apparently.  I did see 2750 RPM before pulling the power back after taking off.  TAS briefly showed over 180 KTAS.  

The "squealer" circuit I put in to remind me to turn off the buss switch didn't activate when getting back to the hangar.  Apparently the voltage on a fully charged battery wasn't low enough for the circuit to trigger.  Looks like there's more work to do on this.  I  think I'd like a way to either temporarily silence the alarm, or improve the logic.

When I was fueling at XBP, a N16KF C150 pulled up.  Out climbed the DPE that gave me my PPL check ride ten years ago!  We chatted about what I'd been doing since then and he admired my Cozy.  He was happy and confided that so many people that got their check rides "hadn't done anything".  

Back at the hangar, I pulled the cowls off in order to change the oil.  I disconnect the lower oil line from the cooler, made a channel out of foil and drain the oil into the oil filler tube.  I've had a few people tell me that the oil drains back into the engine, but I'm getting quite a bit out of the cooler and Vance did this as well.  I drilled a couple holes in the oil filter and blew compressed air in to help the oil drain out of the filter before removing it.  I've had mixed luck doing this so will see tomorrow if the oil drained out.  -Update - there wasn't any oil mess from the oil filter.  Not sure if letting it set overnight or drilling holes in both the bottom and the side were the trick, but anyway, was nice not to have a mess.


Foil guides oil draining out of the cooler and line into the dip stick tube.



Wednesday, November 29, 2023

Balancemaster Dynamic Balancer installed. Lower cowl ramp tweaked.

My wife asked me what I wanted for Christmas and then she told me to order it.  The Balancemaster product was purchased through Aeroperformance/Aircraft Spruce.   This continuous dynamic balancer is rather pricey but it's only a little more than what I'd be charged to for my neighbor to balance the prop once.   Three out of four reviews were good and it comes with a 100 day money back guarantee.  With tax and shipping, was over $400.  https://www.aircraftspruce.com/catalog/appages/lycengblnc1.php?clickkey=8325   

Link to Balancemasters web site:

https://www.balancemasters.com/

This is supposed to fit Lycoming engines behind the prop, in front of the ring gear.  I tried putting it on one way but didn't seem to fit quite right so flipped it around and could see that the Superior ring gear is apparently a little larger.  Based on watching Mike Arnold videos, I'm guessing that this isn't going to have much effect on airflow since the outer diameter is a bit smaller than the ring gear.   There's videos on the Balancemasters web site showing the balancer flipped the other direction, so it should be good.  Rain is forecast tomorrow so might be a couple days before I can test.



The diameter of the balancer is a bit smaller than the Superior ring gear apparently.

I torqued the Saber extension bolts to 50 ft. lbs. and safety wired them.





I tweaked on the lower baffling again.  The #1 & 3 CHT's are within 5%.  The #2 & #4 were within 10% so I added a little piece of glass to divert more air to #4.  The pour foam has made a mess of the lower cowl but I'll clean this up good and make it pretty again.



Frank Bibbee and Vance Atkinson stopped by.

Saturday, November 25, 2023

Trip Report - Auburn KAUO - Thanksgiving 2023

We took off from T67 (Hicks/FTW) Wednesday a little after 0800.  Called KAFW (Alliance FTW) to transition to the East, under Bravo, then headed direct to Minden LA at 7500' for our first stop.  We landed with about 25 gallons so added 8 gallons to give us an extra hour of reserve.  When I'm not doing flight following, I tune up the CTAF of the larger airports as we transit their areas so when Jackson was calling us (unknown AC) out to other traffic, I requested flight following and later got handed off about 5 times and with the exception of Memphis and Atlanta, were fairly quiet.  I got a short GoPro video near Jackson but the battery didn't last long.  



The weather was forecast to be broken near Montgomery but as we got near, the cloud deck below was getting more solid and holes more sparse.  I could make out some water/rivers through some of the holes that were Northeast of Auburn so called Approach to terminate FF and maintained VFR when we were well clear of Montgomery.  I diverted over to one of the cloud canyons and descended under the clouds.  The weather reporting at AUO had been malfunctioning but the Unicom had a jet announce landing on RWY 29.  As I neared the airport, a Citation reported a 5 mile base for 36.  I called that I'd extend my downwind for 36, he thanked me and we followed them in.  I sort of regretted that as there was a bit of turbulence on final.  We slowed and I braked enough that we exited on C.  We taxied to the terminal and were parked in about the same spot as last time with 8 gallons left in the tanks.  We chatted with the line guy about what traffic was going to be like with the Alabama/Auburn football game on Saturday and he confirmed that it gets very busy.  We advised we'd probably be leaving early Saturday due to forecast weather in FTW (rain).  The wind was bumping the rudders so it reminded me to put gust locks on and the exhaust plugs in.  My son helped put the cover on.  And I found later that I left the buss switch on (to raise the landing brake) which powers a relay...and almost drained the battery.  20 gallons of fuel were added.

We enjoyed time with our son & family who fixed a huge Thanksgiving dinner and hosted several dozen relatives.  The weather was great but a bit chilly.

Friday evening some social media posts regarding the airport were made and a temporary NOTAM advised one of the runways would be closed to park aircraft and that a control tower and ground control would be active at 1030.   The forecast weather was still predicting rain in the FTW area Saturday afternoon with ceilings becoming lower.

We got to the airport a little before 0800 and my wife took care of the ramp fee and fuel while my son and I preflighted.  I discovered that I'd left the switch on but the battery wasn't dead yet.  I went ahead and tried a few start cycles but the battery went into protection mode after the third attempt.  My son got jumper cables and the line guys brought a truck over to jump with.  It only took a few minutes to boost the battery and the engine fired up.   I left the nose down and the engine idling to warm up with ambient temp a little above 40F.  I showed my wife how to kill the engine if necessary while I went back in to use the restroom one more time.  My wife climbed into the back and I raised the nose before climbing in.  The oil temp was over 100 now and the amperage was indicating the battery was taking a charge.  I dialed up Montgomery approach and the Unicom before taxiing.  After taking off and calling that I was turning downwind at Auburn, Montgomery approach called my tail number and asked my request....ooops....I was transmitting on Approach.  Oh well...I requested Flight Following to KTVR Vicksburg Tallulah @ 8500.   After passing Montgomery, we descended to 6500 for less headwind.  Fuel burn was a bit higher at the lower altitude.  There's some long stretches of heavily forested areas below and occasionally an Interstate or other roads are visible.  ADS-B wasn't showing much other traffic (filtered to 15 NM/+/- 3500') except when near towered airports.  While en route, KTVR had gone MVFR with haze.  The alternate airport nearby to the south was VFR.  Visibility to the ground as we got further west had dropped to about 20 miles due to haze.  KTVR's ASOS was reporting improved 6 mile visibility and the airport could be seen when I was within 20 miles so discontinued flight following.  We landed and were greeted by a lineman who mentioned my transmit audio was "scratchy".  It's probably because my microphone is to far from my mouth again.  
We got 20 gallons of fuel, took off and requested flight following to T67.  I wasn't sure if  I'd be up to getting entangled with the DFW Class B traffic but it would make the trip shorter if we could get clearance to go direct.   As we passed Monroe, I thought of Paul Roberts and got a quick video of the airport.   As we neared Shreveport, traffic advisories became more frequent and the light cloud layer seemed to be getting lower.  Less than 10 miles from Class B, FTW Center handed me off to a different frequency than I expected, where the controller was in auctioneer mode.  He cleared me into Class B and soon vectored us lower, eventually terminating flight following when we were at 2500 just south of KAFW.   It was 1 PM when we unloaded the plane and was showing 8 gallons remaining.  I did get a few photos of Love Field and DFW. Click on them for a larger image.
Dallas Love Field

Let the fun begin.  Entering DFW Bravo.


After we landed, I got a text from Paul that he'd seen us fly over Monroe!  https://youtube.com/shorts/qS3g4L4JgpI?si=eJ5kcmlpB595JkHA

We unloaded the plane and got a late lunch.  Some items were added to the squawk list.  My wife complained that the rear seat belt attachment was digging into her hip.  I'd heard a squeal that I think is whistle from the canard cover not sealing as well after adding a second Dynon back up battery.  I also want to add an audible warning to alert me when I leave the buss switch on and the engine is not running.  The canopy's (magnetic door switch) contacts seem to bounce when taxiing (and the latch is barely touching the "locked" contact) so I may need to change that to something more robust.  There's a few Dynon configuration items I need to look at as well such as the glide ring not displaying when zoomed out and some other autopilot/Nav settings.  I suspect that when the EarthX battery is charged, it's not smoothing out the electrical noise so either I need to add a lead acid battery or a filter to smooth out the noise...or both.  It would be nice to have a built in boost battery for jump starting or extending endurance should the alternator fail.





Monday, November 20, 2023

11/18/23 Crappy weather=more maintenance

 11/18/23  The sun is finally shining again this morning after having some foggy overcast days.  The weather forecasts were off the mark a bit.  We cancelled a trip to go watch the new SpaceX rocket launch at Boca Chica due weather and other circumstances.  The launch was delayed until Saturday morning.  Maybe we can catch the next one. 

I checked back through log entries and see that the spark plugs had last been replaced in June which was over 100 hours ago.   On my task list was to tweak the fuel settings down a bit and I'd found that the B ECU's mid RPM range values weren't matching the A ECU.  I'm not sure how that happened but am guessing I got interrupted mid-task.  I need to close my hangar door to avoid interruptions when I'm working on tedious tasks.  I reviewed the SDS documents on operation and need to start using the LOP button and get the fuel and timing dialed in for x-country cruising.

EFIS data is showing about a 10% delta on the CHT's.  I'd paused the initiative to get them closer so will attempt to get the balance a little closer.  I'm having to sift through my notes for when and what tweaks I'd made to the lower ramps and now wish I'd added notes to the Savvy flight data.  

The head of a cowl screw stripped so I cut a slot with the Dremel and removed it with a flathead.  Guess it's time for a new batch of screws.

The alternator belt seemed awfully loose even though I'd tightened it recently.  An internet search returned Lycoming SI 1129D and explained how to check the belt tightness.

https://www.lycoming.com/sites/default/files/attachments/SI1129D%2520Alternator%2520Belt%2520Tension%252C%2520Methods%2520of%2520Checking.pdf

Tuesday, November 14, 2023

Friend made a video

 

My friends finally got to go for a ride in the plane they watched me build.  Karen ran the cameras.  Don got to fly and play with the avionics. 



Wheel shimmy and continuing ARINC module going off line

On the task list today:

Check main wheel shimmy source...suspect when I aired the tire up recently that one of the ceramic beads kept the valve stem open and let the air out, flattening the tire and it displaced the tire bead on the rim.  I quickly aired it back up.  Anyway,  I'll jack it up, let the air out, maybe compress the side walls with clamps and then air them back up.  Probably should order new tires and tubes.  On a side note, the new nose tire and lubricated castor bearing has resulted in quieter castoring (no more groaning sounds), but the ride seems to be a bit stiffer when hitting bumps on the taxiway.  Additional note - I'd aired the mains up to 60 psi and found they probably should be at 50 psi.  I replaced one of the filtering valve stems to get the ceramic beads out of it. Update - shimmy is greatly reduced now after setting the pressure to 50 psi in the mains.

The ARINC 429 module is still going off line occasionally and a couple other anomalies at boot or take off.  I'll check power connections that were possibly overlooked (terminal strips under the pilot seat and at the VPX).  Also will see if I have any large filter capacitors in my stock to put near the connector for the transponder, suspecting dirty power is the culprit.  Additional note - found two connectors on the back of the pilot side panel each had the bottom screws loosened on the 15 pin and 37 pin connectors.  Wish these were clips instead of screws. Update - the ARINC module is now staying on line, so apparently the loose connectors on the back of the PFD were the culprit.  I also added a filter capacitor at the essential buss to reduce alternator whine/noise.

SDS had posted some notices, one of which was corrosion on aluminum coil terminals, so will check them and apply dielectric grease. - Update - Found the coil boss inserts were loose and the coil was becoming loose despite the bolts were tight.  I followed the SDS Service Bulletin instructions to resolve that.   There was no corrosion on the posts. 


Relocate pilot and copilot head set jack panels to the strakes near the control sticks.

Pilot side PTT was getting intermittent.  Emailed Tosten and he's sending a new circuit board for the PTT.

Dynon released new software version 16.6.0.10546.  I read the release notes and upgraded the system.  The pilot side panel's fans spun up when upgrading and were growling some.  The copilot side was fine. Need to check into getting new fans.  Update - noticed I was seeing a lot more ADSB targets.  Also, near RPH, saw "Partial ADS-B" which was new.

I'd replaced the bottom plugs but after flying to RPH, getting fuel, the engine still started a bit rough. I just got a new set of plugs, so changed the top plugs too and noticed that the #2 plug that I'd pulled last week didn't look the same as the other plugs, apparently because the gasket wasn't sealing good despite it was torqued to 19 ft. lbs.  

#2 top plug base indicates the gasket wasn't sealing good after the plug was reinstalled.

I found a couple other minor items that I'll address tomorrow.


Friday, November 10, 2023

Thomson Electro-Hydraulic Actuator info

Looking at replacements for the satellite actuator used for the nose gear:


 https://www.thomsonlinear.com/downloads/actuators/H-Track_bruk.pdf



https://www.thomsonlinear.com/downloads/actuators/H-Track_bren.pdf


An email exchange with a Thompson engineer about the H-Track resulted in this model as a possible  replacement:  https://www.thomsonlinear.com/en/product/H2H-12-2A22-A-08


This flap positioning system from Showplanes may work to replace the roller microswitches:

https://showplanes.com/Category/Flap-Position


Bob Morgan is building a LongEZ and has a presentation on implementation of the electro-hydraulic system with a drag link and mountain bike shock absorber:   

https://drive.google.com/file/d/1ko-oGt7l-oznDj-59RlTeDmcSS4XT5yv/view?usp=sharing


Pulled from an email from Thomson:

When it comes to advanced actuator technologies, Thomson has been at the forefront for more than 50 years. That same pioneering spirit exists today amongst our engineers, resulting in breakthrough features and benefits driven by the needs of our customers. To further enhance our offerings and simplify the conversion from hydraulic systems to electric actuators, a groundbreaking set of benefits are driving our latest developments.

FORCE FEEDBACK
For payload-sensing and controlled clamping force applications, Thomson electric actuators can sense an overload event to prevent system damage, push or pull with a predetermined, controlled force level and act as a scale by providing load measurements.

MOTOR/DRIVE/CONTROL & REGEN
For mobile, battery operated applications, regen circuits feed energy back into the battery to extend time between changes, providing more uptime. An integrated motion controller and drive simplify system design and save engineering time, while enabling diagnostics, condition monitoring and bus communication.

POWER DENSITY
For applications with limited space, zero tolerance for leaks or high accuracy requirements, our actuators are suitable drop-in replacements for hydraulic systems, providing efficient weight and space benefits.

SHOCK DAMPENING
For vehicles on rough terrain or applications with impact loads, the actuator's ability to dampen shocks helps avoid breakage of structural machine parts, eliminates bouncing and extends its own service life.

Wednesday, November 8, 2023

Baffling cracks

 At about 150 hours of flight time, 125 Tach.  After returning from formation flying found a couple of cracked pieces of baffle off the #1 and #4 cylinders.  The metal is .032" 2024.   I removed the broken pieces and will see if there's much effect on CHT's.   These parts were cut per plans.  -Update....I think the broken baffles should have been on the outside, not pinched by the screw.  I made new baffles but this time made a lip so the edge clears the screw where the crack occurred and stiffens the part.  A bead of RTV was applied to reduce fretting. 









The new baffle's edge was folded upward to clear the screw and stiffen where it previously broke.




 

The right cylinder baffle clears the 1/4" screw.  A bead of RTV should help reduce fretting.


Tuesday, November 7, 2023

Post flight maintenance 11/7/2023

 A variety of items are cropping up that need attention:
ARIN-429 module, rough running at start up, worn nose tire, relocate headset jacks for pilot/copilot. Found some cracks in baffling - details here:  https://cozy1537.blogspot.com/2023/11/baffling-cracks.html

   

Recently the ARINC429 module was replaced but it seems the transponder was contributing to it going off line.   The coax and connectors for the transponder appear to be good and check good with a meter.  I don't have the TNC adapter to connect to the NanoVNA to see what that looks like though.  There is a BNC connector on the antenna that the Nano will connect to.   Some ferrite beads will be installed on the cables near the antenna to further reduce any stray noise.  Also suspect the annular slot antenna needs a better ground plane.  During Phase I, there was ballast piled around the front of the nose and it has all been moved into the nose.

Thursday evening, Dynon had sent an email alerting of a safety of flight issue with the Auto Pilot panel made 2017 and earlier.  I powered the display up, went into network mode to get the serial number and found it was not an affected unit.  

One of the safety pilots works with avionics a lot and recommended I start the engine with the avionics off, turn on the alternator field, then power up the avionics.  He said that modern avionics are supposed to handle the voltage fluctuations, but after starting the engine, the current and voltages can spike quite a bit.  The downside to doing this is that I cant read my fuel pressure or oil pressure when the engine starts.  I suppose I could boot one display, turn on the fuel pump, then turn the display off while starting.   I'll consult with Dynon support.  It may be with the back up batteries for the displays, they'll help filter the power so may not be an issue.

On Friday morning when starting the engine for the 4th formation flight, the fuel pressure was reading 80 lbs.  I told the safety pilot this wasn't normal so we climbed into his RV7 to do the flight.  Saturday, I pulled the cowls and battery cover.  The ground at the battery was slightly loose and also the positive on the master was slightly loose.  Some of the smaller ground wire screws on a terminal strip in the hell hole took about 1/8 turn.  A test run was good and the cowls were put back on.  I taxied over to the self serve fuel and returned without trouble, shut down and later came back, restarted and the engine was loping and missing terribly.  I pulled the cowls off again, borrowed a spark plug wrench and looked at the top #2 plug.   It looked like it had been pretty wet so suspect the plugs weren't pristine, engine is running a bit rich at lower power settings doing formation flights.  I put the plug back in, did a full power run long enough that the oil had warmed to 200.  It was running fine.  I consulted with several folks about whether it was safe to fly home and I felt it was. 

The nose wheel tire tread has worn down quite a bit on this trip so will probably put a new tire on that is setting on the shelf.  I need to fix the foot on the nose gear too, it's been bent since before OSH when I landed with the gear not completely down.  Mine takes 20 seconds to lower, so the gear needs to come down when entering downwind, not base/final....

 

The "new" tire.
The "new" tire that's been setting on the shelf awhile.

The old Kenda tire.

Fuel filter debris at 150 TT, 70 hours since cleaned last.

The Kenda tire with about 170 landings.



Monday, November 6, 2023

Formation Flight Training at EFD 11/2/2023-11/5/2023

Here's the link to the formation clinic info which has additional links to the FFI's documentation:

https://docs.google.com/document/u/0/d/e/2PACX-1vS4PqgR6T6EDhVn6Ybw7pfy3E_5cjjrhk3YWHT1J5P6BFwHLQ3Cm6DaFf0BlyWe3-jwHy8GlLl9Q0G_/pub?mibextid=S66gvF&pli=1 



Jay Van Every out of Cleburn (CPT) had the opportunity to put some hours on a friend's LEZ so he met me enroute to Ellington (EFD) where the formation clinic was being held.  We planned our arrival for 10:30.   Jay practiced station keeping, crossing under and trail while I led.  Jay was having some avionics issues so was relying on me to navigate and communicate.  We went direct to Cleveland (Northeast of Houston) and dropped under the Class B shelf, then South.  About 25 miles from Ellington I radioed the CT we were an inbound flight of two and position from the nearest airport.  They assigned a squawk code and asked for my location from Ellington which was now about 20 miles NE.  They identified us and confirmed only the lead should squawk.   About ten miles out,  another voice from the tower assigned a new code and advised to report several miles down wind for 17L.  Then as we were nearing closer, a third new voice f rom the tower advised to fly direct to the end of 17L and she'd call our base.  Before we reached the end of the runway, she advised "when able, turn base".  I reduced power, lowered the gear and did an OSH type landing on the 9000' runway with Jay.  We managed to find taxiway Kilo despite it not being marked, taxied to the museum and saw some canards parked already.  When we shut down, Jay said, "THAT LANDING WAS AWESOME!"

Jay & me on the way to KEFD.


Not long after we had parked, Troy Chaddon from Oklahoma taxied a LongEZ in.  

We met Jerry Scott with the museum, Richard Sessions the event coordinator, volunteers (Darlene & Jordan) as well as Scott, a Cozy III builder.

Ryzard Zadow had acquired help from some very experienced folks with a variety of aircraft and planned a four ship demonstration with us newbies riding along to get a picture of what we're striving to achieve.  A LongEZ was lead, with a T-18 as #2, T-34 and RV7 as #3 & #4.  I got to ride in "Bloke's" T-18 Thorpe which was awesome because I'd entertained buying one to fly while I was building.  I was briefly given the stick but tended to overcontrol and started oscillating the pitch.  Yep.  I'm a newbie.   

We debriefed, had lunch and then briefed on doing two ship flights with the ships from the 4 ship flight being lead and carrying observers.  We completed several two ship flights Thursday afternoon.  On my first flight, Bloke was my safety instructor riding in my plane.  On another, Ryz was in the right seat.  I think I was doing better at not over controlling the throttle and pitch but was still to conservative and taking to long to rejoin.  On the first section take off with the T-18 in the lead, I over modulated the throttle right at about rotation and when the T-18 went airborne, we shot ahead as we quickly gained speed when we went airborne.  Ryz called "we were lead" and we coordinated a rejoin.  When we briefed for the next flight, Rodney and Bloke agreed a higher RPM on take off for the RV7 would be good.  With the previous experience, I did better at matching power this time. 

Dynon emailed a bulletin on the Autopilot panel that was classified as a safety of flight issue that showed up in my mail box Thursday evening.  Friday morning, I advised Ryz that I needed to check the serial # before flight and fortunately the serial number was in between affected units.  

Several of us had trouble hearing the tower and I found that I needed to open the squelch on tower frequency when we were at taxiway B.

On Saturday, Rodney was to be my right seater but the Cozy's fuel pressure was reading 80 PSI, which is double what it usually reads.  "This isn't normal...I'm not comfortable taking this on a flight."  Rodney agreed and quickly said we'd take his RV instead.  Flights continued but Saturday afternoon I opted to pull the cowls and work on my plane.  I found a bolt on the large ground cable a smidge loose and one of the positives on the master was a touch loose.  I checked the ground terminal strips in the hell hole and engine bay as well.  Some of the small ground wires on the pilot side terminal strip needed tightened a tiny bit.  Jordan & Richard came over and looked the engine over and took some photos.  I taxied over for fuel and saw the Super Guppy doing touch and goes.  On a subsequent engine start, the engine was acting like the plugs were really fouled.  The cowls came off again a spark plug didn't look bad, but like it had been wet.  The plugs are apparently fouling during the richer start cycle.  A full power test run seemed to be okay so put the cowls back on and chatted with others about if it was safe to fly home.  I was pretty confident after starting, the engine would run fine but I'd need to put new plugs in and tweak the fuel map a bit leaner.

Sunday, Jay & I departed after another formation flight was completed.  We reversed our flight path, so flew to Cleveland, then turned to Cleburn with me squawking 1203 and making advisory calls along the route.  Jay practiced station keeping, finger tip, cross under and trail positions with our KIAS at about 130 and later a little faster after we'd climbed up to 6500.  

We descended to TPA at CPT, did an inspection pass down 15, then right break but I continued North and Jay landed.  I switched the squawk code to 1200, called Meachum for transition clearance to Hicks.  The pattern wasn't busy with a bit of a x-wind out of the West.  

Ryz wanted to know that we'd made it home so I texted Jay first and asked him to text Ryz.  I thought Jay may want to let him know that he'd gotten another hour of practice.

It's nice to be home.

Monday, October 30, 2023

Nebraska Trip #4 Report

 I needed to make another trip to KSNY but this time went solo since my daughter and wife had other plans.  There was enough fuel to easily make it to Clinton OK CLK in 1:10 and then to SNY (2:20).   The weather was beautiful and the MOAs were cold since it was on a Saturday.  I talked with the Tower at Garden City on the Dynon radio and they didn't complain about the audio, so the sensitivity adjustment and mic placement helped.  The plane was put into the transient hangar and 10 gallons of gas was added.  

Several tasks were completed at the farm, but some weren't because the weather turned crappy intermittently on both the departure and destination ends (KSNY-T67).  Initially, I thought maybe I would head back Monday afternoon, but it would have been getting dark at T67 when I arrived and the runway lights aren't as bright as they could be currently.  So I waited the weather out and found a window where it looked like I should be able to get back into the DFW area on Friday afternoon despite cumulonimbus clouds and thundershowers predicted.  

It was cold Friday morning -14F at the farm, then about 28 by the time we got to SNY close to 0900.  I inquired about hangar status as I paid for fuel and storage.  I might still be able to get a T-hangar when someone moves into one of the new hangars, but the completion of the new hangars has been taking longer than expected.  One of my nephews and sisters saw me off.  The heater worked good and when the sun shined into the canopy got even warmer.  I flew to Scott City TQK and this time there wasn't anybody at the terminal, probably because the weather had been overcast.  The ADS-B weather was showing a lot of IFR airports along and to the East of my usual path back towards WWR so I diverted towards Childress to stay out of the MOAs and stayed South of Altus and Sheppard's airspace.  I did monitor traffic and had a couple of Blackhawks in the clouds less than 10 miles from me when I was close to Wichita Falls.  I'd also spotted several flocks of migrating birds (cranes, ducks & others).

I used the Dynon Nearest feature and cycled to the WX tab to see the METAR conditions quickly of the airports along my route.  Graham RPH, Bridgeport XBP, Bowie and Decatur are usually alternates along that route but Decatur was showing IFR.  Bridgeport was showing VFR or MVFR and Graham was VFR.  I'd had to drop down to 2500 MSL and pulled the power back but was still cruising about 150 KTAS.  The visibility was pretty good despite the lower ceiling.  A layer of fog was scattered and was probably around 1500 MSL.  I neared Bridgeport and despite it showing VFR, the scattered fog seemed to be at pattern altitude, yet clearer to the West and South.  I wasn't hearing any traffic at some of the local airports but not surprising as thunderstorms had been passing through to the East.  As I got near Hicks, I could see the airport but also see what was red, yellow and green on the radar.  I crossed the lake and could see the runway but also there was a downpour just south of the runway.   I turned back to the West and got fuel at MWL.  A friend back near T67 confirmed on a phone call that the sun was now shining so 20 minutes later, I landed in sunshine and puddles on the runway.  One of the old timers on the 1st taxiway gestured wings rocking with his arms.  The weather was nice and warm for now.  Three days later, checking Flightaware, I was still the third to last plane to land since the weather got bad again.  I definitely felt blessed to have been able to find that window (using windy.com) in the weather otherwise I'd probably be setting in Nebraska with snow on the ground.



One of the main squawks on this trip is the copilot side display rebooted twice.  The EFIS data does show the voltage changing .1 and the current changed a tiny bit when the screen rebooted.  Not sure if this is a cause or a symptom.  I ordered another Dynon back up battery and will install it today to see if that helps.  Also my ARINC-429 module is supposed to be on it's way back but the shipping number seems to be invalid.  The logged flight time for N724 is now at 150 hours (Hobbs 156 Tach 119.5).  

Saturday, a fellow and his family came out to check out the Cozy.  He'd like to buy one but was wondering how well he'd fit.  He climbed into mine and I forgot to have him put his feet in front of the pedals so he was concerned that his knees would be hitting the panel.  We went over to another hangar where he climbed into a LongEZ and found when his feet were in front of the pedals, he was more comfortable.  

The formation flying clinic is coming up in Houston so I'll make reservations, read the FFI material and prepare for that next.

I also want to add another column to my electronic logbook to count non-solo/passenger flights.

Friday, October 20, 2023

10/19/2023 Flight Review/Com 1 radio transmit noisy/garbled

 My flight review was scheduled at KFWS.  It was a blast to check off some bucket items such as having my CFI fly the plane his student built.  I advised my CFI that it's pretty typical for people to porpoise on their first take off and he did.   We flew to Fredericksburg, happened to se my neighbors logging some time in a C182, had a great lunch and flew back. I think because people are so used to Cessna type yoke forces, they're not expecting minimal control movement.  We did turns and canard stall.  He did a good job landing back at KFWS.  

When I was departing KFWS, Ground advised that the radio was garbled so I switched from Com 1 (Dynon) to the Avidyne and they said it was much better.  I suspect the mic sensitivity needs adjusted along with the mic needs to be placed closer to my mouth.   It's been about 10 years since I taxied to the East side of Spinks so had a little trouble with the taxi instructions regarding crossing and holding.  I'd left my hard copy of the airport chart in my bag in the back so pulled up the chart on Skyview and that helped a lot.

The flight from T67, transition KFTW then into KFWS space is about as busy as you can get working radios.  CTAF at Hicks, AWOS & Tower at KFTW, then AWOS, Tower and Ground at FWS in about 11 minutes in busy airspace.  A radio not working well sucks.  I've gotten used to using the Dynon.  Normally I tap on the airport, hit info, then hit the button to transfer the airport frequencies to the radio panel.   Without this, I was manually plugging the frequencies into the Avidyne.  If a flight plan is entered into the Avidyne, the frequency tab will usually have the destination airport but I haven't seen where it pulls up the ground frequency or AWOS easily.  At some point in the past, I wanted to make a placard with the local Class D tower frequencies so I'll move it up on the list of things to do.